#322 & #323 Dicks Soccer Fields

It has been a long wet spell
So… I was raring to go and up at 4:30 on the second bell. When I got to the field the wind wasn’t noticeable but as soon as I put up the refurbished windsock i could tell there was a strong southerly aloft. This isn’t technically a new site because I’ve flown Dick’s before but this time I’m on the south end instead of the north end of the complex and it is much better. The surface is sand with short and sparse weeds and even though it rained last night the sand was plenty solid enough to walk and fly from. Mike Bennett showed 15 minutes after me and set up closer to the parking area and I’ll do the same next time I’m here.

The first launch was a surprise. I popped up quicker than expected and started to float down but with a little brake I got climbing and started to circle the field while Mike got ready to launch. About 5 minutes into the flight at 1000 feet, I thought, “Did I open the fuel lines?” I had spent longer than normal warming it up and I taxied out to the launch site…AND…I’d been flying for at least 5 minutes. There was no reason to expect that it would still be running but it was and I knew I’d made a big mistake without even looking. When I got twisted around enough to get to the fuel I opened the vent and before I could open the flow valve the motor died.

Now What? I had some altitude, I could try to open the fuel line and restart. I had my doubts though because couldn’t prime the carb. I would’ve had to unbuckle and hang halfway out of the seat to blow into the vent hose, one bump and I’d be swimming. I was in a good place to get back to the LZ and if I fooled around and wasn’t able to restart the motor, it would have been a long push back to where I could re-launch. So…prudence being the better part of valor, I choose to go in “dead stick”. The rest of the story was a non event. I turned downwind, got in position and did a gentle S-turn to bleed off altitude. The landing was smooth but it would have been better if I had taken a wrap to get a little more brake input. It seems like there is a point in the flare where I cannot muscle any more brake. It might be fixable by shortening the brakes.

The second flight was great! Nothing to report.

(Old Stapleton Airport Tower)

(Denver)

(Dick’s Sporting Goods Arena)

Denver to Galveston Pier to do’s

From: Denver, CO 80210 US> To: 2502 Harborside Dr, Galveston, TX 77550-1463
US> > DRIVING DIRECTIONS> ————————————————–>
A) Denver, CO 80210 US> ————————————————–>
1. Start out going SOUTH on S RACE ST toward> E EVANS AVE. (go 0.1 miles)>
2. Turn RIGHT onto E EVANS AVE. (go 0.1> miles)>
3. Turn RIGHT onto S HIGH ST. (go 0.1> miles)>
4. Turn RIGHT onto E ASBURY AVE. (go> 0.3 miles)>
5. Turn LEFT onto S UNIVERSITY BLVD. > (go 0.3 miles)>
6. Merge onto I-25 S (Crossing into NEW> MEXICO). (go 214.3 miles)>
7. Take the US-64 E/US-87 E exit, EXIT 451,> toward RATON/CLAYTON. (go 0.2 miles)>
8. Turn LEFT onto CLAYTON RD/US-64/US-87.> Continue to follow US-87 E (Crossing into TEXAS). (go> 127.3 miles)>
9. Turn SLIGHT RIGHT onto> US-385/US-87/RAILROAD ST S. Continue to follow US-87> S. (go 38.8 miles)>
10. Turn RIGHT onto US-287/US-87/S DUMAS AVE.> Continue to follow US-287 S/US-87 S. (go 46.4 miles)>
11. Merge onto US-87 S via the exit on the> LEFT toward I-40. (go 2.3 miles)>
12. Merge onto I-40 E/US-287 S toward> OKLAHOMA CITY/FORT WORTH. (go 8.4 miles)>
13. Merge onto US-287 S via EXIT 78 toward> FORT WORTH. (go 288.8 miles)>
14. US-287 S becomes US-81 S. (go 30.9> miles)>
15. Stay STRAIGHT to go onto I-35W S/US-287> S. (go 8.9 miles)>
16. Merge onto US-287 S via EXIT 51. > (go 8.4 miles)>
17. Keep LEFT to take US-287 S via EXIT 34A> toward WAXAHACHIE/DALLAS. (go 1.5 miles)> 18. Keep RIGHT to take US-287 S via EXIT 444> toward LITTLE RD/WAXAHACHIE. (go 50.7 miles)>
19. Merge onto I-45 S toward CORSICANA. > (go 246.4 miles)>
20. Take EXIT 1C toward TX-275/HARBORSIDE> DR/FM-188/TEICHMAN RD. (go 0.3 miles)> 21. Stay STRAIGHT to go onto BROADWAY> ST/AVENUE J. (go 0.5 miles)>
22. Turn LEFT onto HARBORSIDE DR. (go> 4.6 miles)>
23. 2502 HARBORSIDE DR is on the LEFT. > (go 0.0 miles)> ————————————————–>
B) 2502 Harborside Dr, Galveston, TX 77550-1463
TOTAL ESTIMATED TIME: 17 hours 19 minutes > DISTANCE: 1079.46 miles> > >
To view your map, click on the link below or copy and paste> it to your browser: > http://www.mapquest.com/mq/3-hUBEfGzFUoKq

Booking #44J0W7
needed:
1)Velcro for Sat Radio
2)Get Regulator checked
3)Binoculars?
4)

321 Simms

Finally a launch before the sunrise !
(Green Mountain)
(home field)

I’ve been trying for weeks and today I finally did it. At 5:30 I turned on the strobes and went up to meet the sun. Beautiful !

Chatfield Reservoir
This had to be one of the best flights of the season. I stayed up as long as possible and would have pushed it till it got thermal if I had the fuel. Even then I put off landing with a touch and go and eventually did the low and slow for the full length of the field before setting down between the wind sock and the truck. It looked good but the wing came down on the sock and broke the pole. Oops.
(home field and beyond ! )

The air was as good as it gets, no bumps and almost no wind. I could barely feel the motor at 2900 RPM. This flight I spent alot of time working the throttle and I think I’m finally getting it. I lengthened the webbing for the foot steering and hooked it up. What a pleasure to have both hands free again! I flew at low RPM and chilled till I couldn’t see any gas in the tank. Terry was right…the more you fly the 4 stroke the more you appreciate it.

(Morrison & Red Rocks)

#319 & #320 Simms

Two very short flights
I’m still trying to get a flight before the sun comes up. Yesterday it was the motor that delayed the launch and today it was the weather. When I got to the field the eastern horizon was just begging to show some color. I had 20-30 minutes before I could see enough to launch and it looked perfect, 65 degrees with calm air. While I was unloading the buggy, the wind started to build. I thought it was going to be the typical little gust front we get so often at sunrise, but it continued to build over the next half hour enough that I couldn’t even kite the wing without being lifted off my feet.So…I sat in the truck and listened to Jazz until 6:30 when it finally started to come down.
Now in full daylight, I launched to the west. The wing came up and the buggy didn’t move. I did the Fred Flintstone / toddler thing and got rolling. By now the wing had fallen off to the left but with some right brake and throttle I was able to recover even though the wingtip was touching the ground. It swung to the right 30 degrees, came back and stabilized. After that the take off was a breeze. Until…I got to 50 feet and encountered very strong turbulence. I could barely penetrate, maybe 5 mph forward and I was being bounced at about a 5 on the bump scale. So I crabbed around to the N. E. corner and landed by the truck. There was definitely a layer because as I descended the buggy started to pick up speed and the air smoothed out. The landing was clean and soft.
The second flight was no different except that the wind on the surface had dropped to 2 mph or less. I thought it had mellowed out but it was still too ratty for my taste. Perhaps I would have found good air at altitude but more likely I would have encountered increasingly higher winds. So… figuring discretion is the better part of valor I called it a day.

318 Simms

New Camera Canon SX200IS

This was a strange one. I got up early so I could launch before the sun only to find that I’d left the ignition on and the battery was dead. I pulled on the starter cord until I was sweating like a dog. This was different: every other time I’ve pull started the 4 stroke, it was a piece of cake. I don’t know if I was just weak or perhaps a circut was switched off …. whatever. I couldn’t pull start it. Two hard inspections didn’t turn up the cause. Eventually I decided to try jump starting from the truck and it fired right up. The motor idled while I set up the wing and when it was time to launch it started on the first pull. Huh? Is there something special about a dead battery that prevents the motor from firing?
The air was good except for a layer at 250 feet that bounced me pretty good during the final approach. The lift off the dam was more turbulant than most mornings. Breeze was coming from the west so I stayed away from Red Rocks and did a lazy loop around the golf course and over by Marston Lake. There was virga in the east and the light was more yellow than usual. Very vivid in the yellows. 45 minutes after launch the wind had shifted from WEST to WSW.

#316 & #317 Meadowlake Airport

Perfectly calm morning! Jerry, Kevin and I delayed taking off for 30 minutes, while we watched Robert (John’s new student) attempt his first flight. No Joy but one hell of an attempt. after two aborted inflations, he got it up ok and was running with the wing stable overhead. Jerry commented that he was a little hesitant on the throttle and I could hear it running up and down. So…Robert got up some speed and was looking good when he jumped into his harness and started to come back down. Amazingly he went to his knees and managed to get back up and keep going without loosing control of the wing. After running right up to the edge of the cut grass he launched and climbed to 10 feet and let off the gas…., eventually coming down too fast to stay on his feet but not so bad that he was injured. Maybe a few bruises but thats it. He’s almost there. Probably next time.
I launched and flew for 40 minutes mostly down low. Jerry came alongside and we explored the north and east side of the area. It was a huge pleasure to fly low and I felt very comfortable. Cruise RPM was about 3200 to 3400 where the vibrations and noise are considerably reduced. Just a great little flight!

#317 was shorter and it was starting to get thermal, I landed before It was even close to being an issue. The wind was picking up above 150 feet where I was only able to penetrate at 8 mph. Coming down to 75 feet I was moving along at 17. Both landings I came in under power to very soft touch downs. Then, Jerry went up in Johns U-turn and seemed to like it… “mostly benign but when you “got on it” the wing became sporty”.

Later we went to Carl Jr’s for a bite and debrief.
Jerry over our freshly cut LZ

//www.youtube.com/get_player

PPG News:

A fellow named Alex is trying to get a google Map PPG site going

http://www.ppgplaces.com/index.php

…It could be great if the bugs get worked out…Stay tuned

314 & 315 Vance Brand Airport

Broke two lines on Eden III Layed out wing wrong.

Ironically I did it the day after I was patting myself on the back for finding the right system. I don’t know why I choose to do it differently …just because I was flying a different wing? The winds were 7 to 9 and it was a smaller wing. I set the trimmers out and probably damped to soon or too much. I wish I had a video so I could see what happened. The buggy was pulled into a partial turtle and came back up before flipping all the way… but the prop caught two lines CM1 and DM1. I think the wing fell back and then surged and folded…if so… I could have saved it if the buggy were accelerating faster. The whole thing would have been avoided if I layed out the wing in a chevron instead of a tight little wall that was like a a coiled spring ready to release. Duh?

I might have been able to avoid cutting the lines with a 2 stroke but the 4 stroke takes a while to wind down. The outer cage ring was slightly bent below the crossbar..I bent it back part way and there is plenty of clearance for the prop. I will probably have to get it welded and true before mounting the New Power Fins.

The TV crew turned out to be a crew from Indonesia. Three people two cameras and a tiny little girl who was either director or translator. It was hard to tell since she never talked to the camera men and could hardly talk to us. Nice …pleasant but not real fluent. Robert and I just kind of went about our business and at the end I gave her my card and she said that she would send me a link after it was edited.

#314 was 40 minutes of tooling around the field waiting for Robert and crew and #315 was a quickie for the camera. It was getting late when they arrived and the air was too thermal for me. I knew it was getting late during take off…I floated above the ground at 5 feet for 300 feet then I entered the lift and was swooped up like a f-16 launch. I hope it made some good video. Robert did some good stuff, nothing hairy some nice hard turns and low level dives and climbs. The swoop divers really looked good. One fellow pulled a 270 between Robert & I and the film crew while we stood about 15 feet apart.

Tomorrow it’s Meadow Lake

#313 Simms

First Sunset Fight of the Season

Finally an afternoon without thunderstorms building over the foothills! I packed and was at the field at 7:30. There as hardly a cloud in the sky and the breeze was half a knot from the south east. I set-up on the high side of the field where the weeds were a bit shorter. There was no problem getting the buggy rolling because of the slight grade and the wing came up perfectly. I think I’ve found the best was to lay out with a slight V and the center tucked up to the cell openings. Take off speed was 24 mph which leads me to think there was a gradient just above the surface.

The light wasn’t great for photography but I tried a 360 degree series anyway.


The air was good with a little mixing going on. I watched a kid practicing motocross for a while and as the breeze built I played with crabbing the wing across the field. When the sun set behind the foothills I turned on the forward strobe. It would be great if I could find a way to turn them both on while in flight. I boated around the field for 20 minutes and when the breeze started to shift to a Westerly decided to land.
For no good reason I was uncomfortable and flew as I expected something bad to happen at any minute. Huh where did that come from? Perhaps it was because I had to sort out a brake line which was not tangled but had wrapped and tightened on the wrong side of the risers. (NON EVENT)
I did have an issue where I had changed the position of the throttle and pinched my hand badly during landing. Part of it might have been because I wasn’t wearing the trusty golf gloves, the “D” ring on the Velcro was pinching the flesh between thumb and forefinger and when I flared it bruised the area behind my knuckles big time.. I’m going to have to sit in the garage and play with it since I’m still having trouble finding a comfortable grip.
PPG NEWS…
Jeff Baumgartner has sold his PPG Plans for Sky Bolt and website to Jeff Goin and his inventory to Terry Lutke. Jeff and Terry plan to keep this excellent design available for pilots who want to build their own. This level of cooperation speaks volumes about their unselfish love of the sport and I applaud them for it.
Bubba has invited everybody to his place next weekend for a midsummer fly-in. I’m bummed, this is the 3rd one that I’m going to miss. Next year for sure!

312 Simms

Launched at 6:00 light air. Flew over to Green Mountain stayed at 1000 ft AGL landed after a touch and go. No Drama. Only bump was when I flew through my own wake. I’m feeling the wing a lot better expecially during landing.

Heard from Terry L. today…the prop has not arrived yet.

Yesterday the interview with Will Jones was posted….it sounded good!