Flight # 1304



Flight # 1304




It was a challenging afternoon that culminated with a hard landing . I did a bit of kiting while the winds settled down. It was variable 5 to 10 cycling about every few minutes. The good news is that lowering the axle 5 inches seems to have done the trick. I’d like a few more launches with a good surface but the prop wash didn’t disturb the wing prior to throttle up.
The landing was terrible. I descended a bit much before final and landed hard. No damage to man or machine. I’m glad there were no witnesses.



The GoPro Max didn’t record and the 11 Black didn’t stabilize…. So much for video.
Notes… yellow lenses for sunset launches. Raise the beaners on the kiting harness.





Good flight except that the wing wasn’t exactly centered and I had to make some fast and dramatic inputs to inflate and center the wing. I’m thinking the narrow opening in the nose of the glider make it easy for the prop wash to inflate one side or the other if not dead on centered.
I’m more convinced that the wash has to be raised to allow forward motion to start the inflation.
Good flight but the wing made a taco during inflation.
Next time I going to try a bit deeper V and tuck up the center to try to keep the prop wash from catching it.






Good Flight
Discovered damaged sheath of main D 3. MD3
Still learning the wing
Raise left hangpoint 1/4 inch
Increase length of A-assists an inch.
Wear smaller brimmed hat under helmet.
Took care to flatten center of leading edge to keep it out of the prop wash and it helped



Starting to feel better about launching.
After the flight I hooked up with Jason Schultz at Safe cove. His Pacific Seacraft is back in the water after 5 months in the yard. We are departing Tuesday to deliver it to its new home up by Bradenton.
Flight #1300
Light winds . First launch was aborted when the wing inflated crooked. The second attempt also required active piloting to get the wing stable overhead.
The video should be helpful.
TRY USING A’assists!



Demo of Nuvik tandem wing



Flew a Nuvik tandem. First impression was that the wing required to much pressure and was sluggish.
No sale
Trike goes Turtle during launch
Pilot achieves 2nd level of the Order of the. Sacred Turtle.
The winds were very light with an occasional puff about 20 degrees to the right of the runway. I set up at the intersection, into the wind, with enough room to turn down the runway after inflation. The wing inflated nicely but while turning developed a mild oscillation. At low speed, I worked to stabilize the wing before committing to launch. During a swing to the right, the wing started a frontal starting left of center eventually dropping the wing to almost vertical. When the inflated side entered the propwash, the trike went “toes up”, very quickly.
Immediately after impact I attempted to stop the motor but the throttle cable had been mashed into the concrete by the lower part of the cage breaking the kill switch wires.
Then ….with the motor running, the trike began to spin while balanced on the prop hub. It completed almost two revolutions before the wing was drawn into the blades, stopping the motor.
Equipment:
Terry Lutke Falcon with 35 hp B&S Vanguard 4 stroke, weighing 248 pounds dry. All up weight, approximately 400 pounds.
MacPara Colorado XXL with approx 350 hours. This wing was well due for inspection and line tuning. I suspected that it was pretty far out of tune due to dragged ) into the sky soaking wet”, many many times the previous spring.
A-assist were not used. Trimmers were set to neutral.
The wing had always been dried and stored in an air conditioned room but the lines were routinely soaked after most flights. There was a tendency of the wing to hang back during inflation. It was very difficult to kite even in stronger air. When new, it had been a great wing easy to kite and fun to fly.




Conclusions
Incident was caused by a couple of pilot errors.




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