New frame looks and fits great.
Prop was near horizontal with three washers on bottom 2 mounts
cleaned up choke,throttle lines with twist split plastic
4 hours to mount engine.
Found and repaired tears in the screen on the air box filters.
Fitted piece of fuel hose over nut which was abrading the filter caps.
Removed battery and had to zip tie switch panel because there are no holes in tubing for battery.
Andy McCavin might not make it due to storm
Author: JoeO
Grounded Again!
Camp Chief Ouray

Aug 31 08 #196

This was a better flight! The air was as smooth as glass, no wind. Take off was perfect…It’s always easier without spectators! I flew to the highway …down valley and up to the pond. The air was sinking over the valley and rising over the ranch. I was suprised to find so much lift this early in the day, the buildings were probably giving off some heat but I think it was probably caused by the exposed earth where they had cut down dead trees. At one point I was still climbing 90 ft/minute at 4500RPM.
The only technical glitch was that the motor was lugging down at full thrust. I descended from 9700 to 9200 ASL and finished the flight keeping the motor below 5400RPM.
Get a 145 and a 148 jet for the carb!
Landing was a surprise…When I got back there was a group of people having church service right where I was planning to land. I was already feeling a little self conscious and didn’t want to draw more attention, so I climbed out and set up an approach that would set me down closer to the horse barn. I was still going to buzz the service but at least I’d be at a higher altitude and not as noisy. The alternate LZ looked good …the grass was a bit higher but it looked good and flat and it was still an easy walk to the truck. What I didn’t realize was, that the grass was high because it was boggy. When the wheels touched down, instead of rolling, they stuck. No roll out at all! I went from 17mph to zero in about 2 feet! It was a rude surprise but I didn’t think it was anything more than a hard landing.
Turns out the frame was damaged, and that was the end of CCO flying… just as well since I got my fix and was free to do other things.
194 Rocky Mountain Balloon Festival



was a blast! It seemed to take forever for the balloons to get off and I waited an additional ten minutes for the Eveready Bunny who should have been named the “never ready bunny”, but eventually it lifted off and Marv. (the safety officer) gave me the thumbs up. The wind was south west so I set up into the wind, pointing to the tree line. The plan worked…I inflated the wing and turned south to line up with the runway. As soon as I was in line, the wing looked good, I hammered the throttle and made a nice clean take off. When I got to the park entrance road I was about 100ft AGL…not great but enough to initiate a hard turn to the right. I did a climbing spiral for several hundred feet and took off to chase the balloons. I crossed Wadsworth and caught up with the pack by the two holding ponds at the south of Chatfield. Everyone except for one lone wolf was skimming the earth, probably trying to collect tags to win the competition. The lone wolf was hanging at about 2000 ft AGL. It was the event organizer and I saw him 45 minutes later heading back toward the port. I was amazed how he was able to come back when everyone else was miles downwind.
I took a few pictures and flew by the CSYC gang who had rafted up to watch the ascension. After 35 or so minutes I returned to the port and tried to land. I was told not to overfly the road so I had to come in from the north east and make a hard turn to final. The way that it slopes down was causing me to come in too high and so rather than land beyond the barrier I choose to set down north of the festival.
I rolled the buggy back to the festival and chatted with Matt and Jerry about meeting some morning to fly at Red Rocks. We said our goodbyes and then Kevin and his family met me at the Marina for a light wind sail.
Balloon Festival 08 Media Day
#192
192 was a morning flight Aug 20th. Chip was going to meet me but had some issue with his reserve and didn’t make it. I put more air in the tires and the buggy accelerated much better, it was rough and the landing was really rough but it helps to reduce the rolling resistance when the field is bumpy. I let the trimmers out and enjoyed the performance of the 28m Eden III. This time I practiced flying lower and after twice getting into bumps to the west at 6300ft went back to the field and areas east. The surprise if the day was broken line on the starboard top cage. I do not think it was a prop strike. The string just broke, maybe I weakened it when I was trying to thread another line to mount the strobe. This afternoon after work before the race I restrung it with 1000lb deep sea line. Much better than factory.
#190 & #191
Simms….70 degrees….light breeze from ENE shifting to NE under light cloud cover
Marek had a hard time making up his mind and when he did decide to fly, he “tweaked his back on a very very long run out. I flew for awhile 15 -20 minutes and landed shortly after I saw Marek land. He was being chatted up by some guy that stopped to watch. Seemed like an OK guy ….Biker”.
After a few minutes of chat the wind had come down to almost nothing so I decided to go up again. The wing came up fine but the buggy was having a hard time getting started, I had to do a Fred Flintstone to get it started but I was too late the glider unloaded and did a frontal. I aborted but the wing came down nicely behind and from the pressure on the risers it felt evenly spread so I grabbed the “A”s” and relaunched without even getting out of my seat. Marek said it looked great. Next time I fly Simms I’ll add a little air to the tires and see if that helps the buggy get started
It was a beautiful flight! Just a few mild bumps to keep me honest.I don’t know why but I didn’t let the trimmers out for the whole flight. Looking back I wished I had because I was paying allot of attention to the way the glider didn’t want to turn into the wind. If I’d just thought about it I could have eased the trim and it would have been a nice sporty ride. But…it was slow and mushy and sometimes mushy is OK.
I spent the last 15 minutes doing touch and goes and flying low and slow. I think I circled the field 5 times before I decided to land. Once in awhile the conditions are right to go to the end of the field and float 2 or 3 feet above the earth all the way to the end.
I learned a good trick on landing. I came in cross the wind about 20 degrees and as soon as I touched down I turned into the wind and used brake to keep the wing turning with me. It will be handy when the LZ is not lined up perfectly for an into the wind approach.
#188 & # 189 Monument Valley
#187 Monument Valley Quick Abort

















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