Colorado Falcon lands in Denver !





The rest of my universe is a total disaster but after months of waiting the Falcon has landed!
I can honestly say this was the first time I’ve smiled in 7 weeks. Pam the u-ship gal showed up an hour early and we unloaded in no time. Best of all she was able to take the Thumper back to Terry on her return trip. He will have it in the first days of Feb.
Quick observations
1. It has the best visibility of any of my previous trikes. I can see all points of the compass. For the first time I will be able to look back through the prop and it will be easy to check fuel level. It will be much easier to launch when I can see the wing inflate without using a mirror. It’s going to be great to be able to look behind and see in all the traditional blind spots. I’m thinking that it will be closer to the foot launch experience. The bucket seat puts you “out there” so… instead of being cocooned inside of a harness or low down in the trike buggy… you’ve got your ”knees in the breeze”, as Brett Cam would say. The forward rail is narrower and the front wheel is out of view which also reduces the “visible stuff” out in front. I’m really looking forward to flying this thing!

2. The bucket seat was a good option, designed for go carts it is very suitable for the Falcon. It fits my small frame great and I think bug guys will like it too. The side rails make great attachment points for the reserve and if I want I can mount a “saddle bag” on the other side for cameras, water, mini parachutes… toys.

3. The electric start was smooth but there is no optional pull start like the Briggs & Stratton. It’s not really an issue… since I never had to use the pull start on the Thumper. Terry relocated the ignition to a central point just forward of the bucket seat. Good move since the first thing I did with the side mount was to break the weld. It also does away with the pivoting arm that the switch was mounted to. Last spring I launched with the hang strap inside of the pivot arm. The strap stressed the arm and I killed the motor trying to sort it out.

4. It’s BIG ! With a 66 inch prop and one piece construction the rig is too big to get inside of my store…except for the front double doors. I can’t get it into the shop for hang testing. So… I’ll just have to stop at an elementary school on the way to my first flight. I probably should have had Terry make it so I could remove the cage but it’s not a big deal. I’ll cope.

5. The 5 point seat belt looks like it came off of a Russian tank. It’s 3 inch webbing with rough cast hardware. When I cinch it up I’ll be able to fly but I won’t be able to reach the GPS or do any weight shift. Most likely after the first few flights I’ll ditch the crotch and shoulder straps. The waist belt is very comfortable and I like the way it snug’s me into the bucket seat. The buckle is primitive but it is a good clean quick release. I’ll braid a lanyard to the Q.R. to make it easy to find in an emergency.

6. I was a little concerned about the wheels but the new mags are bigger than I thought, it will be no trouble rolling over the rough stuff with these babies. Also the rims are split which will make it easy to change out a flat. The front wheel is small so…I might have to use ramps on soft surfaces … Time will tell. I do like the reverse camber of the nose wheel. It will keep it tracking if I decide to be a jerk and take my feet of the pegs… :).

7. The battery came off during transport, so I secured it with zip ties and filled the gap in the battery tray with some stiff closed cell Styrofoam. It will probably benefit from one more Zip tie but it’s not going anywhere the way it is.

I saw God Today #350 & #351 Chatfield

Lucky guy

Intermediate syndrome is an affliction that usually affects a pilot after 40 or 50 flights, or whenever they first start to feel good about their abilities.

It’s characterized by over confidence in both man and machine and it usually leads to a blunder that endangers life. It could present itself in any number of ways… an error in judgement, or a bad reaction to Mother Nature. It might be technique or a mechanical issue. Whatever the cause, if the pilot survives the incident…he should think real hard about either quitting or redoubling his efforts to improve.

It might be time to go to a maneuvers clinic or have some quality radio time with a good coach. It’s absolutely a good day to go over the machine and wing with a fine tooth comb.

Optimistically, there is an epiphany that stays with the pilot for the rest of their career, because on that day… the bag of luck is now half empty and the bag of experience is not yet full.

When I realized that my life was being supported by a glorified key

chain and some thin 1/2 inch webbing…

I thanked the Creator that I was still alive.

Then I looked for the best way,

to proceed to earth…

as directly as possible.

I’m still shaking my head trying to figure out how it happened.I attached the riser on the left side to the cheap plastic beaner that I use for the foot steering instead of connecting to the heavy stainless beaner that ties the wing to the buggy. I didn’t realize my mistake until I noticed that the foot steering cable was pressing against my left side. When I saw that the rig was being supported by a glorified key chain and thin 1/2 inch webbing…I couldn’t believe that I was still alive. Not only was the beaner unrated and not designed to carry a load, the loop it was attached to was loaded against the stitching. There were two places where a failure was imminent. Looking at the materials it should have failed when I loaded the wing before take-off …and… I wish it had. It would have been more dramatic and made a bigger impression but it wouldn’t have killed me. As it was a non-incident, I hope that the magnitude of the error sticks with me.

I had to get down …right now! I was 400 feet AGL and about the correct distance to glide back to the field, so I did a slow flat turn toward the field and landed without incident.

What were the causes that lead to this huge goof ?

1. I had switched to the Eden III which does not require the extra loop of webbing to get the hangpoint right. When it is configured this way the hangpoint loops are not long enough to reach the normal keeper on the bullet bars. So…I end up attaching the beaner to a loop on the foot steering for transport.

2. I must not have had enough coffee because it is almost impossible to imagine an alert mind attaching a plastic carabiner to the riser. It is so much more difficult to thread the correct carabiner that it should have set off alarms when that slim plastic beaner tip slipped through the loop so easily. The length was about right and when I pulled on the riser to take out any slack, it pulled the hangpoint loop just as if it were correctly attached.

I thought perhaps I should move the foot steering forward on the bullet bars to get them away from the hang point straps, but I don’t think I’ll do that. Having the webbing behind my shoulders is cleaner and I doubt I’ll ever look at the foot steering again without remembering the day I hung from a cheap 2 inch plastic carabiner.

This is the first real stupid mistake I’ve made in PPG and certainly the first one that endangered my life! I was deeply affected by the experience, and it was heavy on my mind for several days. I will strive to learn from this and be a more responsible pilot.

I vote for better pilot.

305 Meadowlake Air Park

Great Day Flying above the Clouds!

54 degrees…. Very light breeze from SW…Glass Smooth Air

The take-off was quick despite the humidity and calm air. I flew to the south of the LZ and played with Mathew and Jerry. We were not in close formation but I was close enough to see a big smile on Jerrys face.

I noticed that the RPM’s are dropping to 3450 instead of 3650 which confuses me because the air density should be lower making for higher RPM’s. It might have to do with motor break-in. The climb was an improved 125 ft/min with the PPS 250. I experimented with adding brake pressure and watching the climb increase and practised harder turns.

After Jerry & I split-up I headed South East for about 5 miles climbing all the way to 9237 MSL or 2430 AGL which is a new high for this motor. I saw some low clouds forming in the south and flew to them catching some lift. When I got to the clouds I was 500 feet above them and it was clear that I wasn’t going to get a trophy shot without diving into unknown conditions, so I headed back to Meadow Lake with the clouds chasing me all the way. I landed with 50 minutes of airtime.

For the next 15 minutes we watched the clouds build and were glad to be on the ground. Jerry and Matthew did a little kiting and both commented on their wings hanging back and not wanting to fly….Humidity?

#300

The Big Three Oh Oh
Lucent…Light winds S.E.
I awoke before the alarm…. again …so I decided to check out the new site south of C-470 and west of Lucent. Yesterdays rain had made the freshly graded soil a little slick but I decided to go for it anyway. I was able to lay out the wing without gettingit all muddy but my boots had aquired about 2 inches of clay and the wheels on the buggy were carring a bunch of extra weight. No problem…After I set -up. I just sat in the machine and scrapped the mud off my boots and the wheels. It wasn’t wet, more like clay than anything else.
The climb out was slow but once I was clear of the graded soil and over grass I got some lift and explored the area. This is a pretty good site, enough room to abort, lots of places to set down in an emerency and easy axcess to chatfield. It was mildly bumpy so I didn’t go over to Chatfield next time I’d like to try. I noticed a balloon over the lake and it would be great to play with one of those guys again. The sky looked good but later in the flight I noticed that the clouds were starting to get blown out and I think there was some serious mixing at high altitude.
I did use more brake pressure and that helped smooth things out. It would be great to know exactly how much travel I have in these brakes…I’ll just have to keep pulling more and find out where the stall is.
Landing was a drag….It got real bumpy at 50 feet, it might have been the elevation changes around the field but whatever it was caused me to overshoot and I rolled right into the drainage where the mud was like soup. The wing got a little mud and the buggy weighed a ton. It took an hour to get everything cleaned up back at the house. No damage.
Yesterday I talked with Terry and he is going to start the new cage on Monday. The 64 inch GSC Prop should boost my climb rate considerably.

Chad’s High Altitude Test Flight

Way to go Chad
12,000 MSL

While I was getting my ass kicked at Vance Brand Chad was setting a new record for the 4 stroke Trike Buggy

Here is his report…
Re: 12000′ 4stroker climb out
Posted by: “trikebuggydelta” http://us.mc01g.mail.yahoo.com/mc/compose?to=chad@TrikeBuggy.com&Subject=trikebuggydelta
Mon Mar 2, 2009 10:01 am (PST)
Thumper High Altitude TestsI went out to El Mirage and the Flying “J” Ranch this last weekend tofly the Thumper. I wanted to launch and land the machine, maybe ahundred times, and really get a feel for it. I wanted to do some highaltitude tests, to see how high it would go and what the climb rateswould be at different altitudes. I got there Friday afternoon, and pulled the Thumper out of my shedand gave the key a try. BrBrBRrBrBr, it sounded like a jackhammer as Irealized that I should have removed the positive battery lead before Ileft last time. I pulled my Toyota over near the Thumper and gave herthe breath of life. I let the Thumper run for close to an hour,letting her charge the battery up so I had a bit of reserve. The greatthing about the Briggs & Stratton motor is that this thing just runs!You simply start it, and it just loves to run. I changed the throttlea few times to 2000 and 3000 RPM, and sometimes I would run it rightup to full (at the pitch I had the IvoProp at, it topped out at around3400 RPM – should have been around 3800), then let her rest at around1200 idling. Finally, started setting up for a flight. Wrong! Once I got in theair, I could see why the Quicksilver Ultralight pilot looked so amused- it was punchy! On the ground, it was maybe 0-4 mph, seemingly niceconditions, but once in the air it was a different story. I did a fewgo-arounds and decided that it was a bit much for me and landeduneventfully. I spent the rest of the afternoon installing the FootSteering, a Reserve Parachute, more velcro for the instruments,getting some more gas and generally tightening everything andpreparing for the evening flight. At just before sunset, I launched again, and enjoyed maybe 30 touch &go’s before it got so dark I was squinting to see. I was flying theDudek Synthesis 34 glider, and it worked beautifully with all thatThumper weight (220lbs) dangling from the lines. I trimmed this reflexglider full slow for this flight, and it inflated perfectly everytime(5 inflations) with the A-Assists and was still fast in the air.Looking at the risers, I saw that full slow is actually a bit slowerthan trim speed, so I set the trimmers at 0 (there’s actually numberson the trimmer) to put the glider at true neutral for the morning flight.Jerry Frost and Pierre Beney arrived this evening, and we spent a goodbit of time ‘Hangar Flying’ around the campfire, watching the moon setalong with that planet, really spectacular!The next morning, I warmed the Thumper up for flight. With the twistof the key, she stirred to life and seemed to be content. I let herrun for a good half hour at idle, something I would never do to any ofmy two-strokes (they would coke-up and choke) while I prepared forgoing high. I used a Flytec Vario for climb rate, a Garmin GPSmap 76for better altitude, and my iPhone with the V-Cockpit app running, avery cool airplane instrument application that uses the internal GPSfor navigation. Only problem was the iPhone was so dim that is didn’tcome out in the pictures. You can see one shot of it in the photogallery on the Altitude screen, just one of the many functions thisapp has. Check out the main screen by clicking the small icon here toyour right. It’s a really cool Application, and I had fun playing withit as I flew. There’s even graphs of the entire flight showingaltutude, speed, climb rate, heading, but no way to save them! At about 8:30, I launched from the Flying “J” Ranch at approximately2850 feet and velcro strapped the throttle at full and sat back andrelaxed, took pictures, video, and wrote down info at each 1000 feetof altitude. On this first flight, I did not write the time down, butyou can see the time on the pictures of the GPS, so it tookapproximately one hour to climb to 8000 feet and 1:25 to climb to12,000 feet. I was still climbing at 12000 feet, but very slowly, andI was cold – I didn’t wear enough layers to keep out the chill. Plus,I had not pitched the prop for maximum efficiency, at ground level itwas only 3400, and it got slower as I climbed. The motor ran beautifully the whole time, not even a hiccup. I amamazed by the four-stroker’ s incredible reliability. I could get usedto this! Trouble is, when I fly a two-stroke again, I’ll be wonderingwhen it will happen…. the inevitable motor-out. This motor is madeto run, and run, and RUN! I let it idle for a few minutes after Ireached 12K, then shut it down for the long glide back down. I reallyenjoyed the views from up high, there was snow on the nearby peaksnear San Bernadino, and I could see all the way to Tehachapi to thenorth and into the LA basin through the El Cajon Pass.

260 261 262 Thumper’s maiden Voyage

I was a little nervous laying out the wing but the motor started like a champ and the Thumper took off just fine. The brake pressure required was alot more than I was used to. and I didn’t like the way the buggy was pitching. Chad didn’t think there was anything to worry about but I’m not liking it. After landing Jerry Frost made it a point to tell me that I needed to raise the hang points because I was wheelbarrowing during launch.
The second flight was very short. The machine was so quiet that I forgot to put in plugs and put on the helmet. Right after lift off The hat went through the prop and when I heard the “wack” I was thinking broken prop or worse. I got off the throttle quick and came out of the dive with just barely enough time to flare. I bounced floated and landed. I write that one off to unfamiliar equipment and move on.
The third flight was pretty good. I stayed up maybe 30 minutes and experimented a bit with the wing. It’s really hard to pull. There is plenty of power at sea level . I’ll know more when I get a chance to fly in Colorado.
//www.youtube.com/get_player

251 252 253 254 255 256 Salton Sea

Big Day lots of firsts…

Most Flights in one day. It should probably be 256.5 because I did a touch and go that was so long I taxied the full lenght of the field.

First time to fly a performance wing Spice 24 (or there abouts)
First time to fly a 4 stroke. I took up Bens machine with the eden 28.

The thumper flight was marred when I rigged the brake line thru the hangpoint rings and had a friction lock. Landed dead stick at the rocky end of the field. I had to take a wrap on the Brake line above the ring.

Tonight there was a prop burning and outdoor movies.

I had dinner with Ben at the Mexican Resturant…Huge Special plate.

Flight 225 Simms

A small milestone

It’s looking allot like the end of the season and in a couple of days I’m going to have my knee repaired…So…I REALLY WANTED TO FLY TODAY. Weather Underground was predicting 15 mph NE and later NW winds. Away from the foothills and out on the plains it look better with 4 to 5 mph. I was looking for places in Aurora and trying to find the old Aurora Air Park on google and map quest and decided to drive out east and take my chances. On the way home I noticed that the wind was considerably less than predicted. I decided to try Simms and sure enough there was a very light breeze 1 to 3 mph from the ENE. Perfect !

I set up and launched at 290 degrees. The wing came up wanting to turn left and it changed my intended bearing so that I was pointing right at the truck when I took off. Fortunately it was a non event because I had marched far enough out into the field so that I would be able to clear or turn once in the air. Later I realized that I had let one trimmer out an inch before taking off which explains the cockeyed launch. Some thing must have distracted me because I know to do things like that in pairs to keep things symmetrical. Anyway, I flew trimmers out as well and in this flight I really like the firmness of the wing with the trimmers out but the mixing air got me to thinking it was better to play it safe.

The air was smooth except for a few spots. I’ve noticed that when I get into rowdy air, I have a tendency to turn away and seek clear air instead of plowing through and getting to the other side of whatever is mixing the air. It really wasn’t that bouncy but I was leery of the cut in the mountain and what could be flowing down the hill. So I turned and ran toward the home field. What I should have done was to turn 90 degrees and then when the air was good turn back to the direction I wanted.

When I was back over the field I did some low passes and apparently scared a dog who ran away from it’s owners. I didn’t know about it until I landed and met the family. Their little boy who was probably 13, approached me right away and asked if I’d seen their dog. I felt terrible when I met his mother and she said my PPG is what spooked him. I remembered flying right over the lady at maybe 30 feet. She was concealed by her truck until I was within 100 feet. I remember thinking, “That’s not Cool”, but I don’t make a practice of flying over people, it was just one of those things” …I wished it hadn’t happened and apologized sincerely. She was very cool about it and said there was no way to know that the dog was going to react that way. I think she had more warning of me than I had of her and probably would have been able to secure her dog if she had thought it was necessary. At least I hope so …

So I offered to go back up and look which she was all in favor of. The wind had shifted to the WSW and for some reason the wing hung back and came up crooked. I aborted when I started to feel it pulling.

Huh…maybe I’m finally starting to get a feel for the wing.

A breakthrough at 225 flights!

Anyway… I aborted the first attempt and when I was collecting the wing …What should come on to the IPOD that was playing random songs? ….John Blacks near fatal accident. It was just the audio but that got my attention.

I could hear the paramotor clearly in the background and the camera man was saying oh o…oh shit…. John? Well it caused me to pause and when I set up the second time Damn if the wing didn’t do the same thing coming up off to the side. I probably had room for one more attempt but the sun was getting low and I decided to call it quits. The lady still hadn’t found her dog when I pulled out. I’ll give her a call tomorrow to see what happened.

It was a nice long flight ! Over 50 minutes and if I hadn’t heard some strange sounds from the motor I would have stayed longer.
I spoke with the owner the next day and…they found the dog!

Fight 200 at Simms

The Stock market is bouncing like a super ball…Nobody is buying pianos…. but Today…I celebrate the big 200.

Unfortunately it was not a real noteworthy flight. Launched from Simms at 6 pm. The skies were sporting some bug cumulous and there was the threat of virga to the Northwest. I climbed to 6400 6500 and tested the footsteering. It works but there is too much friction. It’s slow and sluggish. I am getting more travel and the wing turns quicker but it just doesnt feel right yet. I should have tried it with the trimmers out but I’ll leave that untill the next time.

Time to replace the Tach.

Motor is hard to start the first time ,then it’s ok.
The Monument Valley Gathering is next week….4 days till I leave.

#145

Very nice morning flight! 145 isn’t a magic number but it is the 100th trike flight and two weeks short of a year since the El Puerco Fly-in when I switched to wheels. I tried something a little different with set-up. Instead of laying the wing out in the butterfly configuration I used the thrust line to partially inflate the wing before I sat down. It pulls the risers all the way back to the cage but it’s not hard to separate the “A”s and get into position. The wing comes up fast and smooth and you need to use a little brake because it wants to overshoot… but I liked the feel of it and will try it again. Several of my last take-offs have been pretty ugly and I think it’s because I’m rolling out at too high a speed. This morning wasn’t too bad a launch but I was at take off speed very quickly and the first little bump wanted to pop me into the sky. It would be easier to modulate speed on a smoother surface than this bumpy field but I know it will help if I can slow down…stabilize the wing and then go to full throttle.

The air was smooth most of the flight. There was a little turbulence approaching Red Rocks Park which dissuaded me from trying to drop into the park and fly between the fins. I’ll do it someday when I can launch at the crack of dawn and be well into the park while the air is dead still. Probably not a good place to fly after the rocks have been cooking in the sun all day. I can imagine cool air flowing down the Rockies mixing with the warm air rising from the rock.

Downtown Denver was shrouded with early morning humidity and I was even able to see Chatfield off to the South.

After going west I turned to the east of the LZ and flew over the School, Jail and Southwest Shopping Center.It took awhile to descend from 2000 feet and I was surprise to encounter sinking air and bumps over the LZ